Sunday, November 8, 2009

Removed the Satellite radio and the HD radio from the glove box. Added a Bluetooth interface for the iPhone so I can play iPod or Pandora/Internet radio and take calls through the stereo.

Sunday, October 11, 2009

Oil Change!

Royal Purple and Purolator.

Thursday, September 24, 2009

EGR?

Well maybe we've got this thing close to being acceptably licked. I took the EGR valve off and put a calibration disc in that's about two sizes smaller than the one called for in the instructions. The I tried replacing the 5-way ported vacuum switch, but managed to break the new one. Not having a special socket for the task, I decided to put the old one back in for now, ordering both a new switch and a socket to make a special tool out of, and drive the car in the meantime and see how the recalibration works. Well it works very well! I don't have nearly the amount of hesitation when the valve opens as there was. I'd say in most cases it's imperceptable. BUt even when you can feel it, it is very slight. I'll leave it at that. The replacement ported vacuum switch may help even more, but if not, I think it is OK the way it is. Otherwise, I think the next step is to get the carb rebuilt with an eye to the ported vacuum tap being carefully investigated. You should be able to adjust the idle speed and not get into the range where vacuum starts pulling at that port. And it shoudln't be a sometime thing, but consistant.

Friday, September 11, 2009

More EGR issues!!!

This morning on the way to work, the EGR was really making the engine run rough and bog down. It woudl nearly die at stop lights and buck when I gave it a little gas. But eventually it smoothed out and I went to work without much further fuss. On the way home, all seemed well until I got off the freeway, then it was pinging like crazy and the idle was high... like no EGR at all.

I already had run into trouble with the 5 port vacuum port switch not running the Thermac system properly. It was allowing vacuum to the heat/cold door on the air cleaner snorkel when the engine was hot, which made the engine ping like crazy. I moved it to another port that is not used on my car where vacuum is cut off at the same time vacuum is turned on to EGR. And now this!

I ordered a different brand of vacuum port switches (yes, both the 3 and 5 port switches) and hopefully this will solve the problem. Once that is resolved, I think I need to either put the original EGR valve back in the car or recalibrate the new one with a different metering disc. It seems to be a bit too heavy on the exhaust gas intro. That or the carb needs to be rebuilt. What a mess!

Monday, August 10, 2009

Salerno's Auto Air

Sometimes it takes a little help from a professional. I took Helen over to Salerno's Auto Air and showed them my problem. Terry pointed out that the thin tube would overheat and melt before the thick block it was attached to would let the braising material melt to seal the crack. He figured it was better to get a replacement part. I left the car with him all day and he found one replacement part, put fresh hose on it, charged the system and found no other leaks. I think we're back in business. :D Blows nice and cold again.

Sunday, August 9, 2009

A/C Leak

No luck on the A/C leak. It seems there is a second problem that is due to a tiny crack where the aluminum tube is brazed onto the block that attaches at the back of the compressor. Wow, no chance of getting a replacement any time soon. I guess I will have to break down and take the car over to a shop that can repair the crack. It would be so nice to have a spare to drop off and have refreshed with barrier hose, but I can't drive tha car in this heat anyway. Phooey!

Saturday, August 8, 2009

A/C

Well, it may not be the o-rings on the compressor that are leaking after all. When the car was converted to use 134a, the kit they used had a high pressure adapter that has a 90° swivel bend in it. I was checking to see if it was loose and it turns out it was. I started to tighten it down but then though I'd better check the o-ring in it... voila! The o-ring is toast.
Closer inspection reveals that this o-ring is even more critical than usual on an adapter. The adapters I've seen are straight and very short. They do not have their own schrader valve but rely on the original R-12 valve. The o-ring in these adapters is only to seal when charging the system. As soon as the hose set is removed from the adapter, the original core seals shut and the o-ring does nothing, essentially. But because this adapter has the bend, the original core was removed and there is a schrader valve in the adapter instead. The o-ring now has to hold pressure all of the time, not just when charging. And with the swivel, it has to be a perfect seal or it leaks like crazy. Copper flare-nut type swivels, which this is similar to, can be really tightened down to seal and the soft copper will crimp itself to the shape needed to seal as you go tighter. But you can only tighten this swivel down so far before the o-ring distorts and tears... exactly what happened.

Off to Pep Boys for a replacement high side adapter... of course they only had the pair in a full conversion kit. No matter, it included a new schrader valve core, which I was going to need as mine had been removed. The bend in the old adapter had made it easier to connect the charging hose, but I found that it wasn't much more trouble to connect with the straight stubby one though. The seal will be so much more reliable it will be well worth any minor inconvenience anyway.

Right now I have a 15 in vacuum pulled on the system and I'm waiting to see if it holds. I had already ordered an assortment of o-rings and if the system won't hold the vacuum I'll need to wait for them to arrive before I can charge. But I think these o-rings are OK. For one thing, the compressor is a rebuilt unit and the rings are green, so they are correct for 134a. They can't be that old!

Saturday, August 1, 2009

Thermal Vac Switches

Replaced the two thermal vacuum port switches that manage all the smog control devices. I seem to have them back to working in harmony again now.

Unfortunately, when I charged up the A/C system I found that the compressor is leaking at the back where the hose pad connects. Probably just the o-rings but now I need to find a set that work with 134a.

Saturday, July 25, 2009

More EGR Investigation

After following the troubleshooting steps in the manual, I see the two ported vacuum thermal switches are bad. The full manifold vacuum that goes into one port is getting sent all the way back up the chain to the ported vac connection on the carb, screwing up pretty much everything. I can get new ones easily, about $35 each. In the meantime, I have plugged the manifold vac hose which seems to only affect the thermac door on the aircleaner.

Tuesday, July 21, 2009

EGR Issue

I'm having an issue with my '76 regarding the EGR valve operation. The old valve was weak, so was letting exhaust gas pass even with no vac signal. I replaced it with a new valve and it turns out the real problem is that it is getting a vac signal even at idle, so the idle is real rough when the hose is connected. I went all the way back to the carb and it seems the ported vacuum point on the carb body has vacuum at idle too, so the various temp switches are just passing it on. Ported vacuum should be zero at idle, right? Is the Q-Jet due for a rebuild then?

Sunday, June 14, 2009

Passenger side mirror finally correctly aligned and functional! I had gotten a electric unit off of an '80s Buick some time ago and replaced the manual, dealer mounted original. I had even made a space in the dash for the control and ran the wires over to the right A-piller. But that was where it sat for quite a long time. But recently I found the head was coming loose and the angle has never been right anyway, having adapted the '80s car mounting arm to the '76 door in a not so great way. Again, quite some time ago I had gotten a correct, cable-controlled '76 model mirror on eBay, figuring I'd use the correct arm when I got around to wiring up the mirror the rest of the way. So this was the weekend make it all come together. New arm nicely mated to the '80s electric head and wired up so it's working beautifully. I tapped the power and ground for it from the clock, as it was convenient and close by.

Friday, May 22, 2009

Radiator

New radiator arrived tonight and Installed it along with a new lower hose. I have not completely buttoned things up and I need to buy coolant to fill the system tomorrow. But hte major replacement is done.

Wednesday, May 20, 2009

Radiator Again

Over the weekend, I tried to make the small leak of coolant stop, still assuming the drips were due to a trucculent hose clamp. But after double-clamping and still no joy, I decided the best choice is to either have a pro investigate, or just bite the bullet and order a replacement radiator. I just replaced the original a year ago with a new 4-row job. But it really looks like the seam on the right tank is weeping and with hot weather on the way, there is no room for a system that won't hold pressure. So I figured what the cost would be of having a pro look at it and determined I was going to save money by just getting a new radiator, new lower hose and new clamps, plus some coolant. I can then see if it's worthwhile to have the old radiator repaired and set aside as a spare.

Saturday, May 2, 2009

Coolant Overflow Tank

Helen's original tank, which was molded into the fan shroud, was leaking and was also in the way of things. My solution was to replace it with an aftermarket job, but I didn't want a cheesey plastic add-on type, so I got a cheesey tuner add-on type instead. At least it's metal and will hold up pretty well. Disadvantage, it's kinda small for this big ol' engine. We'll see how well it works. I think I have another leak somewhere else as well.




Sunday, April 19, 2009

Headlight adjustment screw for the up/down swing of the high beam on the right side broke and I had to put a new one in today.